An experimental Study of a two dimensional inlet model in non-uniform supersonic flow are presented.
介绍一种二元进气道模型在非均匀超音来流中的初步研究结果。
By comparison of inlet total pressure recovery coefficient, attack-angle performance of chin inlet and two-dimensional inlet are superior to frontal inlet.
对不同布局的总压恢复系数进行比较,颌下及两侧进气则较头部进气有好的攻角特性。
And three-dimensional sidewall compression inlet with 25 percent cowl position has high mass capture and total pressure recovery coefficient and isolator exit flow flied is homogeneous.
整流罩位置为25%的三维侧压进气道可以获得较高质量捕获和总压恢复系数,且隔离段出口流场比较均匀。
In this paper, a FVM-TVD method for simulation of one-dimensional unsteady flow in inlet and exhaust manifold of ICE has been constructed.
介绍了进排气系统一维非定常流动的FVM-TVD法(总残差减少的有限体积法)。
The results show that the actual turbulent round jet flow must be simulated by a three-dimensional analysis with inlet perturbations.
分析了不加扰动和加扰动模拟的本质差异,指出准确预报实际圆湍射流流动应采用施加入口扰动的三维模拟。
There is a difference between the numerical simulation results of two-dimensional and three-dimensional flow field in supersonic inlet, which shows the influence of boundary layer on the side wall.
超声速进气道的三维流场数值模拟结果与二维数值模拟结果存在较明显的差别,说明进气道侧壁附面层的影响不容忽略;
The three-dimensional simulation model of the spiral inlet duct of a diesel engine is created with the FIRE software, and CFD simulation of inlet flow is carried out.
利用FIRE软件建立了某柴油机螺旋进气道的三维仿真模型,对进气流动进行了CFD模拟计算。
A numerical simulation of the three-dimensional steady flow field in the whole flow field, from the inlet of the collector to the outlet of the diffuser, a 2k70 axial-flow fan is performed.
针对2k70型轴流式通风机从集流器进口到扩散器出口的内部三维全流场做了定常的数值模拟。
The two-dimensional MHD controlled inlet in the accelerator mode is numerically simulated, and the influence of some key parameters on the performance of the inlet is analyzed.
采用二维磁流体动力学(MHD)模型对加速器模式的磁控进气道进行了数值模拟和参数优化。
A fixed-geometry two-dimensional mixed-compression supersonic inlet with sweep-forward high-light and bleed slot in an inverted "X"-form layout was tested in a wind tunnel.
针对一种带放气槽的定几何二元倒置“X”型混压式超音速进气道进行了风洞吹风实验。
A fixed-geometry two-dimensional mixed-compression supersonic inlet with sweep-forward high-light and bleed slot in an inverted "X"-form layout was tested in a wind tunnel.
针对一种带放气槽的定几何二元倒置“X”型混压式超音速进气道进行了风洞吹风实验。
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